A Simple Orthogonal Set-screw Tuning Method to Improve Periodic Error
Email: michael.blaber@med.fsu.edu
Author biography:
Abstract
The following article describes a cheap and simple method of
minimizing a substantial portion of the periodic error in a typical worm drive.
The method makes use of orthogonally positioned set-screws on both ends of the
worm. Appropriate pair-wise adjustment of these set-screws permits the addition
and subtraction of sine and cosine functions, of variable magnitude, to the
worm period. These functions can be applied in combination, like a simple set
of Fourier terms, to progressively eliminate a majority of the periodic error.
Introduction
Perhaps my back yard is similar to that of other amateur
astronomers. There is an area, overgrown now, where I placed three 12"
round aggregate pavers, spaced to accommodate my old 6" reflector's
tripod. Next to this is a 4ft2 concrete slab that I poured, to
permit me to easily reposition my old 6" reflector's tripod (since I erred
in positioning the aggregate pavers to permit polar alignment of the
telescope). Next to the slab is an 8 x 10ft roll-off roof observatory (which
elicited only a single formal complaint to the local homeowner's association)
with a half-ton concrete base into which is permanently mounted an 8"
diameter steel pier to support my present telescope (a 12" Schmidt Cassegrain). These stages of construction reflect my
growing interest in astrophotography (although my wife was concerned that they
might also reflect stages of progressive cognitive impairment).
After several years of working with my mass-market 12" Cassegrain I began to appreciate both the strengths and
weaknesses of the system. On the one hand, the capability that the telescope
was astounding: automated star alignment, periodic error correction, GoTo feature, computer interface, etc., combined with
excellent optics, and affordable price. On the other hand, I came to the
conclusion that the limitation of the system for astrophotography, was not the
optics but the mount; the key limitation being the accuracy of the right
ascension drive. In short, errors in the right ascension drive were causing
slightly oval star shapes (the long axis being east/west). Despite
disassembling the drive base, installing new bearings, cleaning the gears,
etc., no amount of simple tinkering could substantially improve matters.
I came to the conclusion that mass market telescope
manufacturers probably achieve a desired level of tracking performance by a
carefully managed interplay between the mechanical and electronic subsystems.
If the system were mechanically precise, there would be no need for electronic
measures to correct for tracking error; however, such mechanical precision must
be extremely expensive to achieve. Conversely, inexpensive electronic circuitry
can only do so much in attempting to compensate for mechanical error. So, there
must be an economic balance: reasonable mechanical precision, and reasonable
electronic correction, for overall reasonable cost. Although the images I was
recording amazed me, the slight oval shape to the stars became more and more
irritating; and I realized that I could do no more with the mount that I had.
In short, it was time to invest in a more mechanically precise mount.
I had always wondered why some mounts cost more than the
optical assembly; now I could appreciate the value of mechanical precision.
Unfortunately, purchasing a truly high-end mount was simply not an option. My
wife was blissfully unaware of how much I spent on my telescope, and there was
no way I was going to tempt fate twice by siphoning our savings for an expensive
mount. Furthermore, it is difficult to explain to others why it is essential
that images of stars be round instead of slightly oval. I began searching the
web for suppliers of accurate (yet reasonably priced) gear and worm sets with
which to build a more accurate mount. There was not a lot to choose from. To
make matters worse, there were conflicting degrees of apparent user
satisfaction with certain suppliers. I settled on a 2" shaft diameter
pillow block assembly with a 9" right ascension gear and 1" worm
(6" gear with 1/2" worm for the declination drive) from a supplier
that quoted a high-degree of accuracy and listed a large number of prior
customers (presumably satisfied).
Assembling the mount and drive has been a time-consuming and
arduous task that so far has consumed the better part of a year (and is still a
work in progress). Among the various issues faced during this past year: 1) a
need to find a manufacturer of custom 2" bore gears for 6mm belts to drive
shaft encoders; 2) the supplied 1rpm DC motors were wholly inadequate (even
after purchasing a regulated power supply and building a sensitive pulse width
modulator) - I opted for an installation of Mel Bartel's
servo motor system; and 3) design and machining of a spring-tensioned mounting
block for the right ascension worm (the solid mount design provided was not
precise enough). Finally, when it looked like I could see the light at the end
of the tunnel, it turned out to be a lightening strike that fried my computer's
serial port, shaft encoder and the servo controller (ah, summer in Florida...).
Mel is one heck of a guy and replaced the servo controller; the other parts
were, unfortunately, out of warranty.
At long last, the time had arrived to check out the periodic
error of my new mount; although it was still summer in
Several anguished days went by, after which I was finally
able to think a little more clearly. I concluded that there must be a good
reason why the error was so great (other than I had been savagely ripped-off by
the gear manufacturer). The periodic error looked very much like a cosine wave
with the peak, curiously, near the exact start of the worm period. After
examining the worm gear, and the reference mark I had made, I noted that the
mark was, coincidentally, adjacent to one of the two set-screws that secured
the worm to its shaft. Was it possible I had applied too much torque while
tightening the worm set-screws? Considering that the entire mount assembly
(including wedge and OTA) weighs around 400 pounds, some bolts require heavy
duty torque when tightening. But the worm set-screws were fairly small and
delicate, and perhaps I had been too aggressive when tightening them; I decided
to loosen them (what the heck). They did not seem particularly tight, and I
loosened them to what seemed to be a bare minimum of torque to retain the worm
on its shaft. After another endless wait for clear skies, I plotted the
periodic error. A dramatic improvement! The "wave" had subsided
noticeably to a height of about 30 arc seconds peak to peak. Things were moving
in the right direction, but I could do no more since the set-screws were about
as loose as I dared make them. What I needed was a set-screw on the opposite
side of the worm that I could tighten.
The Hypothesis
I thought about the problem for several more days. It was
possible that the worm shaft was out of round, and that the set-screw issue was
merely a way to compensate for this eccentricity. Alternatively, the worm axis
might not be exactly parallel to the worm shaft, and the set-screw adjustment
provided a means to make fine adjustments to align the axis (the two set-screws
on each end of the worm were 1800 opposed to each other). Thus, the
hypothesis I was contemplating (because of the observed effect of the set-screw
adjustments upon the periodic error) was that the worm set-screws not only
affix the worm to its shaft, but also determine its alignment with the shaft
axis, and misalignment contributes significantly to periodic error. If
this hypothesis was correct, then the course of action was obvious: I would
need to tap threads for additional set-screws in the worm to permit additional
adjustments. In particular, I would need a series of four orthogonal set-screws
at each end of the worm. The worm shaft would also need four orthogonal flats
filed or machined at each end to accommodate the set-screws. Another agonizing
moment of truth: do I drill, tap and grind two of the most holy parts of the
mount (using my really cheap drill press), or do I content myself with a
periodic error that is going to irritate me in perpetuity?
Figs. 1 and 2 illustrate the ultimate course of action that I
took. The worm gear was marked to indicate 0, 90, 180 and 2700
reference points (Fig. 1) coincident with the four orthogonal set-screws at
each end of the worm (Fig. 2). The eight individual set-screws are identified
by their corresponding angle referenced on the worm gear, and which end of the
worm they are located (my worm is oriented east/west on the mount and the
set-screws are identified as being either "east" or "west").
Figure 1.

The
right ascension worm shaft and drive gear. Orthogonal flats have been machined
into the shaft for the four set-screws on both ends of the worm. The alignment
of the set-screws and their corresponding position in the worm period are
marked on the worm shaft drive gear. In this particular mount the end of the
shaft nearest the drive gear is "East".
Figure 2.

The
worm with four orthogonal set-screws tapped into the hubs at both ends of the
worm (and with identical alignment).
The test
To begin the great experiment, each set-screw was tightened
to a bare minimum torque to affix the worm to its shaft, and then a healthy
torque (I don't own a torque wrench) was applied to the 00W and 1800E
set-screws. The periodic error (a whopping 50 arc seconds peak to peak)
comprised a cosine wave (i.e. a trough at 1800 and a peak at 00
(Fig. 3)). I then loosened the set-screws again and tightened the orthogonal 900W
and 2700E set-screws. The periodic error (a similarly huge 40 arc
seconds peak to peak) now comprised a sine wave (i.e. with a trough at 2700
and peak at 900 (Fig. 3). My excitement at these results was
difficult to contain; the worm set-screws
could be used to adjust the worm alignment on the worm shaft in a controlled
manner. I had at my disposal the ability to add or subtract sine and cosine
functions, in any combination and magnitude, to minimize the periodic error
(Fig. 4).
Figure 3.

The
right ascension tracking error with the worm initially mounted using only the
set-screws at the 00W and 1800E positions (magenta trace), or at the 900W and 2700E
positions (orange).
Figure 4.

A listing of the various orthogonal
set-screw adjustments of the worm and the corresponding effect upon the worm
tracking error.
Starting over, and with an initial periodic error
approximately described by a cosine function (Fig. 5), I applied a negative
cosine function by gently tightening the 00E and 1800W
set-screws. After repeating this (since the initial adjustment was
insufficient), the residual periodic error was now approximately described by a
sine wave (Fig. 5), and so I applied a negative sine function by tightening the
900E and 2700W set-screws. At this stage the periodic
error started to resemble a slight negative cosine function and, therefore, a
very slight cosine function was applied. At this point, the required
adjustments were mere nudges on the set-screws, and it was easy to over-shoot
the adjustment. The final periodic error has been reduced to approximately 6.5
arc seconds peak to peak, with a standard deviation of 2.7 arc seconds (Fig.
5); this is substantially better than my previous mount *after* electronic
periodic error correction. It may be possible to improve upon the current
periodic error by the application of a slight sine wave, but the run-to-run standard
deviation is approximately 2.5 arc seconds, so any further improvement will be
marginal (but must be attempted nonetheless!).
Figure 5.

Progress
of the tracking error as corrective sine and cosine functions are applied using
the different set-screws in the worm: 1. Initial periodic error (magenta); 2.
After application of an initial (-) cosine function (red); 3. After further
application of a (-) cosine function (green); 4. After application of a
subsequent (-) sine function (blue); 5. After addition of a corrective (+)
cosine function (black).
In short, the right ascension gear and worm assembly do
indeed have the accuracy that was stated by the manufacturer (sorry about all
the rotten things I was thinking...); however substantial effort was required
in achieving it. For systems with accessible, shaft-mounted worms, the
orthogonal set-screw tuning method described in this report can substantially
reduce periodic error with little to no financial cost.
(c) 2005 Dr.